Palm Beach International Airport
Aircraft Accident/Incident Report

West Palm Beach, Florida 33406
Friday, September 3, 1999 3:25 EDT

NTSB Narrative Summary Released at Completion of Accident

At 0314, the pilot reported to the Air Traffic Control (ATC) Tower that he wanted to divert from his destination to land at a closer airport, and was cleared for a visual approach. At 0325, the pilot issued a "Mayday." On final approach the airplane struck a building and wires about 1/2 mile short of the runway. Witnesses that saw the airplane just before impact said that the airplane was low, there was no in-flight fire, and the engine sounds "...appeared to be a fluttering sound as if air [was] passing through the propeller." The pilot had filed for a cruise altitude of 15,000 feet, with a time en route of 5 hours, and fuel on board 6 hours. Weight and balance calculations showed that the pilot was operating about 722 pounds above the maximum gross weight for the takeoff, climb, and maximum cruise power settings. The Pilot Operating Handbook calculations showed that most of the fuel would have been used during the flight. The engine and propeller examinations revealed that both engines were not producing power at impact (windmilling). There were no discrepancies found with the engines or propellers. Examination of the propellers revealed that they were not in the feather position and they were not in beta/reverse position. Line personnel at the departure airport confirmed that all the tanks were topped off (282 gallons added). It took the flight 32 minutes to reach a cruise altitude of 15,000 feet, which calculated to about 293.3 pounds (1 gallon of Jet "A" equals 6.7 pounds), and a flight time of 4.9 hours from takeoff to impact. Sample calculations indicated that the fuel burn rate would have caused the airplane to use 2,649.3 pounds of Jet "A" turbine fuel during the flight. The flight departed with all tanks full 384 gallons usable (2,572.8 pounds), which calculates to insufficient fuel for the completion of the flight. Two gallons of fuel was drained from the right nacelle tank at the crash site, and there was no evidence of in-flight leakage. The sample calculations do not consider performance degradation for operating the airplane above the maximum allowable gross weight, which would cause the fuel consumption to go up because more power was required for the over weight conditions. The pilot's flight plan was for economy cruise, plus the airplane was over gross weight at takeoff, and there are no performance charts for that condition. So, the performance was even poorer than shown on the maximum power chart for climb and cruise. Calculations of the maximum allowable fuel that could be on board the aircraft showed that only 1851 pounds of turbine fuel could be carried to start the flight at the maximum allowable weight, or about 3.2 hours of flight. The en route winds aloft at the airplane's altitude indicated a slight tailwind for half the flight and a headwind of about 15 knots for the remainder of the flight.

NTSB Probable Cause Narrative

a total loss of engine power due to fuel exhaustion. Contributing factors in this accident were the pilot's operation of the airplane in an overweight condition, inadequate pre-flight and in-flight planning.

Event Information

Type of Event Accident
Event Date 9/3/1999
Event Day of the Week Friday
Time of Event 325
Event Time Zone Eastern Daylight Time
Event City WEST PALM BEACH
Event State FLORIDA
Event Country --
Zipcode of the event site 33406
Event Date Year 1999
Event Date Month 9
MidAir Collision Indicator No
On Ground Collision occurred ? No
Event Location Latitude --
Event Location Longitude --
Event Location Airport PALM BEACH INTERNATIONAL
Event Location Nearest Airport ID PBI
Indicates whether the acc/inc occurred off or on an airport Off Airport/Airstrip
Distance from airport in statute miles 1
Degrees magnetic from airport 310
Airport Elevation 18
Weather Briefing Completeness Unknown
Investigator's weather source Weather Observation Facility
Time of the weather observation 340 Eastern Daylight Time
Direction of event from weather observation facility (degrees) 130
Weather Observation Facility ID PBI
Elevation of weather observation facility 18
Distance of event from weather observation facility (units?) 0
Time Zone of the weather observation EDT
Lighting Conditions Night/Dark
Lowest Ceiling Height 0
Lowest Non-Ceiling Height 3500
Sky/Lowest/Cloud Conditions Scattered
Sky Condition for Lowest Ceiling None
Visibility Runway Visual Range (Feet) 0
Visibility Runway Visual Value (Statute Miles) 0
Visibility (Statute Miles) 10
Air Temperature at event time (in degrees celsius) 73
Dew Point at event time (in degress fahrenheit) 68
Wind Direction (degrees magnetic) 0
Variable Wind Indicator Unknown
Wind Speed (knots) 3
Wind Velocity Indicator Unknown
Wind Gust Indicator Unknown
Wind Gust (knots) 0
Altimeter Setting at event time (in. Hg) 29
Density Altitude (feet) --
Intensity of Precipitation Unknown
METAR weather report --
Event Highest Injury Fatal
On Ground, Fatal Injuries 0
On Ground, Minor Injuries 0
On Ground, Serious Injuries 0
Injury Total Fatal 8
Injury Total Minor --
Injury Total None --
Injury Total Serious --
Injury Total All 8
Investigating Agency NTSB
NTSB Docket Number (internal use) 10313
NTSB Notification Source --
NTSB Notification Date Sep 3 1999 12:00AM
NTSB Notification Time 345
Fiche Number and/or location -used to find docket information IMAGE
Date of most recent change to record Jul 30 2001 11:11AM
User who most recently changed record MONR
Basic weather conditions Visual Meteorological Cond
FAA District Office --

Aircraft Involved

Aircraft #1

Aircraft Registration Number N338AS
NTSB Number MIA99FA245
Missing Aircraft Indicator N
Federal Aviation Reg. Part Part 91: General Aviation
Type of Flight Plan filed IFR
Flight plan Was Activated? --
Damage Destroyed
Aircraft Fire Ground
Aircraft Explosion None
Aircraft Manufacturer's Full Name Beech
Aircraft Model B-90
Aircraft Series Identifier B-90
Aircraft Serial Number LJ-493
Certified Max Gross Weight 9650
Aircraft Category Airplane
Aircraft Registration Class U.S. Registered/U.S. Soil
Aircraft is a homebuilt? No
Flight Crew Seats --
Cabin Crew Seats --
Passenger Seats --
Total number of seats on the aircraft 9
Number of Engines 2
Fixed gear or retractable gear Retractable
Aircraft, Type of Last Inspection Annual
Date of Last Inspection Apr 5 1999 12:00AM
Airframe hours since last inspection 75
Airframe Hours 8832
ELT Installed Yes
ELT Activated No
ELT Aided Location of Event Site Unknown
ELT Type --
Aircraft Owner Name C.P. HORIZONS CORP
Aircraft Owner Street Address 5300 W. ATLANTIC AVE
Aircraft Owner City DELRAY BEACH
Aircraft Owner State FL
Aircraft Owner Country
Aircraft Owner Zipcode 33484
Operator is an individual? --
Operator Name
Operator Same as Owner? Yes
Operator Is Doing Business As --
Operator Address Same as Owner? Yes
Operator Street Address
Operator City
Operator State
Operator Country
Operator Zip code
Operator Code
Owner has at least one certificate None
Other Operator of large aircraft? No
Certified for Part 133 or 137 Operation Unknown
Operator Certificate Number --
Indicates whether an air carrier operation was scheduled or not --
Indicates Domestic or International Flight --
Operator carrying Pax/Cargo/Mail --
Type of Flying (Per_Bus / Primary) Executive/Corporate
Second Pilot on Board Yes
Departure Point Same as Event No
Departure Airport Code PTK
Departure City PONTIAC
Departure State MI
Departure Country
Departure Time 2231
Departure Time Zone EDT
Destination Same as Local Flt --
Destination Airport Code BCI
Destination City BOCA RATION
Destination State FL
Destination Country
Specific Phase of Flight --
Report sent to ICAO? --
Evacuation occurred --
Date of most recent change to record Jul 16 2001 8:32AM
User who most recently changed record dbo
Since inspection or accident --
Event Location Runway Number and Location 13
Runway Length 6931
Runway Width 150
Sight Seeing flight No
Air Medical Flight No
Medical Flight --