Mckellar-Sipes Regional Airport
Aircraft Accident/Incident Report

Jackson, Tennessee 38301
Sunday, June 3, 2001 16:11 CDT

NTSB Narrative Summary Released at Completion of Accident

About 20 minutes before the accident, the pilot reported to the air traffic controller that he had a problem with an engine and needed to shut the engine down. The flight had just leveled at 23,000 feet. The controller told the pilot that he was near Jackson, Tennessee, and that he could descend to 7,000 feet. About 10 minutes later, the pilot reported he was at 8,000 feet and requested radar vectors for the instrument landing system approach to runway 2 at the McKellar-Sipes Regional Airport, at Jackson. The pilot told the controller he had the left engine shut down. About 5 minutes later, the pilot reported he had a propeller runaway. About 1 minute later, the pilot reported he was in visual conditions and requested radar vectors direct to the airport. About 2 minutes later, the pilot reported he had a cloud layer under him and that he had the localizer frequency for runway 2 set. About 1 minute later, the pilot was told to contact the McKellar Airport control tower. The pilot acknowledged this instruction. No further transmissions were received from the flight. Examination of the left engine at the accident site showed the left propeller control was found disconnected at the point the propeller control extension bracket attaches to the propeller governor. The propeller control cable had also pulled loose from a swaged point at the control rod and was also separated further aft due to overstress. The housing for the propeller control rod was found securely attached to the engine and the control rod was securely attached to the extension bracket. The propeller governor control arm, which was disconnected from the propeller control cable and rod, was found spring loaded into the high RPM position. Examination of the fractured left propeller bracket assembly was performed by the NTSB Materials Laboratory, Washington, D.C. The bracket assembly was fractured in the area of the outermost eyehole, at the point a bolt passes through the bracket assembly and the propeller governor arm. The fracture surface contained small amounts of dirt, grease, and minor corrosion. The fracture surface features include flat areas that lie on multiple planes separated by ratchet marks, features typically left behind by the propagation of a fatigue crack. The fatigue crack emanated from multiple origins on opposite sides of the bracket. The total area of the fatigue crack occupied approximately 85 percent of the fracture surfaces. The fatigue fractures initiated on the outer edges of the surface and propagated inward toward the center. The remaining 15% of the fracture surface had features consistent with overstress separation. Near the middle of each fatigue region were micro-fussures suggesting that the crack propagated under high-stress conditions. The NTSB Materials Laboratory also examined the separation point between the left propeller control flexible cable and the rigid rod that connects to the bracket assembly. The cable and the swaged part of the rigid rod were in good condition with no fractures or damage. The Piper PA-31-T2 Pilot Operating Handbook, Section 3, Emergency Procedures, does not contain a procedure for loss of propeller control. Section 3 did contain a procedure for "Over speeding Propeller", which stated that if a propellers speed should exceed 1,976 rpm, to place the power lever of the engine with the over speeding propeller to idle, feather the propeller, place the engine condition lever in the stop position, and complete the engine shutdown procedures. Pilot logbook records show the pilot completed a simulator training course for the accident model airplane about 9 days before the accident and had about 13 flight hours in the Piper PA-31-T2.

NTSB Probable Cause Narrative

The pilot's shutting down the left engine following loss of control of the left propeller resulting in an in-flight loss of control of the airplane due to the windmilling propeller. Factors in the accident were the failure of the propeller control bracket assembly due to fatigue, the pilot's lack of experience in the type of airplane (turbo propeller) and the absence of a procedure for loss of propeller control in the airplane's flight manual.

Event Information

Type of Event Accident
Event Date 6/3/2001
Event Day of the Week Sunday
Time of Event 1611
Event Time Zone Central Daylight Time
Event City JACKSON
Event State TENNESSEE
Event Country --
Zipcode of the event site 38301
Event Date Year 2001
Event Date Month 6
MidAir Collision Indicator No
On Ground Collision occurred ? No
Event Location Latitude 352944N
Event Location Longitude 0885414W
Event Location Airport McKellar-Sipes Regional
Event Location Nearest Airport ID KMKL
Indicates whether the acc/inc occurred off or on an airport Off Airport/Airstrip
Distance from airport in statute miles 8
Degrees magnetic from airport 180
Airport Elevation 434
Weather Briefing Completeness Full
Investigator's weather source Weather Observation Facility
Time of the weather observation 1553 Central Daylight Time
Direction of event from weather observation facility (degrees) 360
Weather Observation Facility ID MKL
Elevation of weather observation facility 434
Distance of event from weather observation facility (units?) 7
Time Zone of the weather observation CDT
Lighting Conditions Day
Lowest Ceiling Height 2400
Lowest Non-Ceiling Height --
Sky/Lowest/Cloud Conditions --
Sky Condition for Lowest Ceiling Overcast
Visibility Runway Visual Range (Feet) --
Visibility Runway Visual Value (Statute Miles) --
Visibility (Statute Miles) 10
Air Temperature at event time (in degrees celsius) 18
Dew Point at event time (in degress fahrenheit) 17
Wind Direction (degrees magnetic) 60
Variable Wind Indicator Wind direction could be determined
Wind Speed (knots) 4
Wind Velocity Indicator --
Wind Gust Indicator Not Gusting
Wind Gust (knots) --
Altimeter Setting at event time (in. Hg) 29.88
Density Altitude (feet) 1000
Intensity of Precipitation Light
METAR weather report --
Event Highest Injury Fatal
On Ground, Fatal Injuries --
On Ground, Minor Injuries --
On Ground, Serious Injuries --
Injury Total Fatal 5
Injury Total Minor --
Injury Total None --
Injury Total Serious --
Injury Total All 5
Investigating Agency NTSB
NTSB Docket Number (internal use) 12429
NTSB Notification Source
NTSB Notification Date Jun 3 2001 12:00AM
NTSB Notification Time 1815
Fiche Number and/or location -used to find docket information DMS
Date of most recent change to record Oct 23 2002 10:24AM
User who most recently changed record NTSB\MONR
Basic weather conditions Visual Meteorological Cond
FAA District Office Memphis

Aircraft Involved

Aircraft #1

Aircraft Registration Number N31XL
NTSB Number MIA01FA152
Missing Aircraft Indicator --
Federal Aviation Reg. Part Part 91: General Aviation
Type of Flight Plan filed IFR
Flight plan Was Activated? Yes
Damage Destroyed
Aircraft Fire Ground
Aircraft Explosion None
Aircraft Manufacturer's Full Name Piper
Aircraft Model PA-31-T2
Aircraft Series Identifier --
Aircraft Serial Number 31T-8166003
Certified Max Gross Weight 9474
Aircraft Category Airplane
Aircraft Registration Class U.S. Registered/U.S. Soil
Aircraft is a homebuilt? No
Flight Crew Seats --
Cabin Crew Seats --
Passenger Seats --
Total number of seats on the aircraft 8
Number of Engines 2
Fixed gear or retractable gear Retractable
Aircraft, Type of Last Inspection Annual
Date of Last Inspection Jul 11 2000 12:00AM
Airframe hours since last inspection 61.2
Airframe Hours 6025.8
ELT Installed Yes
ELT Activated No
ELT Aided Location of Event Site No
ELT Type --
Aircraft Owner Name Falcon Communications, Inc.
Aircraft Owner Street Address 1708 N. Douglass
Aircraft Owner City Malden
Aircraft Owner State MO
Aircraft Owner Country USA
Aircraft Owner Zipcode 63863
Operator is an individual? No
Operator Name --
Operator Same as Owner? Yes
Operator Is Doing Business As --
Operator Address Same as Owner? Yes
Operator Street Address --
Operator City --
Operator State --
Operator Country --
Operator Zip code --
Operator Code --
Owner has at least one certificate None
Other Operator of large aircraft? --
Certified for Part 133 or 137 Operation --
Operator Certificate Number --
Indicates whether an air carrier operation was scheduled or not --
Indicates Domestic or International Flight --
Operator carrying Pax/Cargo/Mail --
Type of Flying (Per_Bus / Primary) Executive/Corporate
Second Pilot on Board Yes
Departure Point Same as Event No
Departure Airport Code MAW
Departure City MALDEN
Departure State MO
Departure Country USA
Departure Time 1525
Departure Time Zone CDT
Destination Same as Local Flt --
Destination Airport Code FTY
Destination City ATLANTA
Destination State GA
Destination Country USA
Specific Phase of Flight Maneuvering
Report sent to ICAO? Yes
Evacuation occurred No
Date of most recent change to record Sep 30 2002 3:47PM
User who most recently changed record KENJ
Since inspection or accident Time of Accident
Event Location Runway Number and Location 2
Runway Length 6008
Runway Width 150
Sight Seeing flight No
Air Medical Flight No
Medical Flight --