Southwest Michigan Regional Airport
Aircraft Accident/Incident Report

Benton Harbor, Michigan 49022
Sunday, August 4, 2002 13:35 EDT

NTSB Narrative Summary Released at Completion of Accident

The single-engine airplane experienced a loss of engine power during cruise flight at flight level 190 (19,000 feet) and impacted the terrain while performing a forced landing to a nearby airport. Visual meteorological conditions prevailed at the time of the accident with clear skies and unrestricted visibilities. The pilot reported the loss of engine power about 16 minutes prior to the accident and requested clearance to the nearest airport. Air traffic control (ATC) issued vectors to the Southwest Michigan Regional Airport (BEH). About 10 minutes prior to the accident, the airplane was positioned approximately 1.3 nm north of BEH at 13,500 feet. The pilot elected to follow ATC vectors verses circling down over BEH. ATC provided vectors for runway 27 at BEH. Witnesses to the accident reported seeing the airplane "spiraling down and crashing into the ground." The wreckage was located on the extended runway 27 centerline, about 1.12 nm from the runway threshold. The distribution of the wreckage was consistent with a stall/spin accident. Approximately four minutes before the accident, the airplane was on a 9.5 nm final approach at 6,700 feet. Between 9.5 and 5.3 nm the airspeed fluctuated between 119 and 155 knots, and the descent rate varied between 1,550 and 2,600 feet/min. Between 5.3 nm and the last radar return at 1.5 nm the airspeed dropped from 155 to 78 knots. According to the Pilot Operating Handbook (POH) the accident airplane should be flown at best glide speed (92 knots) after a loss of engine power. An average engine-out descent rate of 700 feet/min is achieved when best glide speed is maintained during engine-out descents. An engine teardown inspection revealed that the crankshaft was fractured at the number five crankpin journal. Visual examination of the crankshaft (p/n 13F27738, s/n V537920968) showed a fatigue-type fracture through the cheek, aft of the number five crankpin journal. The exact cause of the crankshaft failure could not be determined, due to mechanical damage at the fatigue initiation point. The fracture features for the accident crankshaft was consistent with 14 previous failures of the same part number. The engine manufacturer determined the failures were most likely due to the overheating of the steel during the forging process.

NTSB Probable Cause Narrative

The pilot's failure to maintain airspeed above stall speed resulting in a stall/spin. Additional causes were the pilot not maintaining best glide airspeed and optimal glidepath following the loss of engine power. A factor to the accident was the engine failure due to the fatigue failure of the crankshaft.

Event Information

Type of Event Accident
Event Date 8/4/2002
Event Day of the Week Sunday
Time of Event 1335
Event Time Zone Eastern Daylight Time
Event City Benton Harbor
Event State MICHIGAN
Event Country --
Zipcode of the event site 49022
Event Date Year 2002
Event Date Month 8
MidAir Collision Indicator No
On Ground Collision occurred ? No
Event Location Latitude 420739N
Event Location Longitude 0862342W
Event Location Airport Southwest Michigan Regional
Event Location Nearest Airport ID BEH
Indicates whether the acc/inc occurred off or on an airport Off Airport/Airstrip
Distance from airport in statute miles 1.12
Degrees magnetic from airport 95
Airport Elevation 643
Weather Briefing Completeness Full
Investigator's weather source Weather Observation Facility
Time of the weather observation 1335 Eastern Daylight Time
Direction of event from weather observation facility (degrees) 275
Weather Observation Facility ID BEH
Elevation of weather observation facility 643
Distance of event from weather observation facility (units?) 1
Time Zone of the weather observation EDT
Lighting Conditions Day
Lowest Ceiling Height --
Lowest Non-Ceiling Height --
Sky/Lowest/Cloud Conditions Clear
Sky Condition for Lowest Ceiling None
Visibility Runway Visual Range (Feet) --
Visibility Runway Visual Value (Statute Miles) --
Visibility (Statute Miles) 10
Air Temperature at event time (in degrees celsius) 31
Dew Point at event time (in degress fahrenheit) 22
Wind Direction (degrees magnetic) --
Variable Wind Indicator Variable
Wind Speed (knots) 4
Wind Velocity Indicator --
Wind Gust Indicator Not Gusting
Wind Gust (knots) --
Altimeter Setting at event time (in. Hg) 30.12
Density Altitude (feet) 2480
Intensity of Precipitation --
METAR weather report --
Event Highest Injury Fatal
On Ground, Fatal Injuries --
On Ground, Minor Injuries --
On Ground, Serious Injuries --
Injury Total Fatal 3
Injury Total Minor --
Injury Total None --
Injury Total Serious --
Injury Total All 3
Investigating Agency NTSB
NTSB Docket Number (internal use) 16468
NTSB Notification Source FAA
NTSB Notification Date Aug 4 2002 12:00AM
NTSB Notification Time 1430
Fiche Number and/or location -used to find docket information DMS
Date of most recent change to record Oct 28 2004 10:11AM
User who most recently changed record NTSB\MONR
Basic weather conditions Visual Meteorological Cond
FAA District Office FAA - South Bend FSDO

Aircraft Involved

Aircraft #1

Aircraft Registration Number N316PM
NTSB Number CHI02FA231
Missing Aircraft Indicator --
Federal Aviation Reg. Part Part 91: General Aviation
Type of Flight Plan filed IFR
Flight plan Was Activated? Yes
Damage Substantial
Aircraft Fire None
Aircraft Explosion None
Aircraft Manufacturer's Full Name Piper
Aircraft Model PA-46-350P
Aircraft Series Identifier --
Aircraft Serial Number 4636317
Certified Max Gross Weight 4340
Aircraft Category Airplane
Aircraft Registration Class U.S. Registered/U.S. Soil
Aircraft is a homebuilt? No
Flight Crew Seats --
Cabin Crew Seats --
Passenger Seats --
Total number of seats on the aircraft 6
Number of Engines 1
Fixed gear or retractable gear Retractable
Aircraft, Type of Last Inspection Annual
Date of Last Inspection Nov 1 2001 12:00AM
Airframe hours since last inspection 187.2
Airframe Hours 187.2
ELT Installed Yes
ELT Activated Yes
ELT Aided Location of Event Site No
ELT Type --
Aircraft Owner Name Danny Lee Williamson
Aircraft Owner Street Address 3220 Millstone Court
Aircraft Owner City Maumee
Aircraft Owner State OH
Aircraft Owner Country USA
Aircraft Owner Zipcode 43537
Operator is an individual? Yes
Operator Name --
Operator Same as Owner? Yes
Operator Is Doing Business As --
Operator Address Same as Owner? Yes
Operator Street Address --
Operator City --
Operator State --
Operator Country --
Operator Zip code --
Operator Code --
Owner has at least one certificate None
Other Operator of large aircraft? --
Certified for Part 133 or 137 Operation --
Operator Certificate Number --
Indicates whether an air carrier operation was scheduled or not --
Indicates Domestic or International Flight --
Operator carrying Pax/Cargo/Mail --
Type of Flying (Per_Bus / Primary) Personal
Second Pilot on Board No
Departure Point Same as Event No
Departure Airport Code FSD
Departure City Sioux Falls
Departure State SD
Departure Country USA
Departure Time 1000
Departure Time Zone CDT
Destination Same as Local Flt crash at destination city
Destination Airport Code BEH
Destination City Benton Harbor
Destination State MI
Destination Country USA
Specific Phase of Flight Emergency descent/landing
Report sent to ICAO? No
Evacuation occurred No
Date of most recent change to record Sep 10 2004 8:37AM
User who most recently changed record SULP
Since inspection or accident Time of Accident
Event Location Runway Number and Location 27
Runway Length 5109
Runway Width 100
Sight Seeing flight No
Air Medical Flight No
Medical Flight --