Aircraft Accident/Incident Report

N. Fort Myers, Florida 33903
Thursday, June 26, 2003 12:51 EDT

NTSB Narrative Summary Released at Completion of Accident

The pilot reported visually checking the main fuel tanks during his preflight inspection of the airplane and later reported there was enough fuel for the intended flight which would be less than 1 hour, plus a 45-minute reserve amount of fuel. He estimated the fuel level in the main fuel tanks was 2-3 inches from the top. He also reported that before the accident flight he had never flown the accident make and model airplane, and that he had not had any flight training in the airplane. The passengers were boarded, the flight departed and climbed to between 4,500 and 6,500 feet msl. He leaned the mixture during cruise, and the flight continued. He began descending when the flight was 12 miles from the destination airport, and he performed the pre landing checks when the flight was 3 miles from the destination airport. The flight entered left downwind where he lowered the landing gear and turned on the fuel pumps. When abeam the landing point he reduced power, lowered the flaps 10 degrees, and turned onto base leg. During the base leg while rolling out of the turn and flying at 600 feet, "the right engine suddenly came to a stop...." He banked to the left to maintain zero sideslip, pushed the mixture, propeller, and throttle controls full forward, and identified the right engine had failed. He reportedly pulled the right propeller control to the feather position but during the postaccident investigation, the right propeller blades were not in the feather position and there was no evidence of preimpact failure or malfunction of the propeller. The pilot further reported that while pulling the right propeller control to the feather position, the airplane, "began to yaw right and simultaneously bank right...." He moved the left throttle control to idle, and they were on the ground in a span of 6 seconds from the time the right engine quit. No fuel leakage was noted at the scene, and no fuel contamination was noted in a nearby pond. Additionally, only residual fuel was noted in the fuel lines in each engine compartment. A total of 4.0 and 1.5 gallons of fuel were drained from the left and right auxiliary fuel tanks, respectively. No evidence of preimpact flight control failure or malfunction was noted. Neither propeller was at or near the feather range at the time of impact. Both engines were removed from the airplane, placed on a test stand with a "club" propeller, and both engines were noted to operate normally during the engine run. Examination of the right seat in the third row of the airplane revealed the seat frame was bent down on the left side, and all seat feet were in position but distorted; no fracture of the seat feet were noted. Examination of the seat of the passenger who sustained minor injuries (left seat in the third row) revealed the seatpan was compressed down, and the lapbelt was unbuckled. The inboard arm rest was bent inward, and the outboard arm rest was bent outward. The seat frame indicated displacement to the left. The seat back was twisted counter clockwise, and the left forward seat foot was in place. The seat and attach structure was certificated for a maximum forward g loading of 9 g's, and a maximum sideward g loading of 1.5 g's. This does not include a 1.33 margin of safety factor. The seat and attach structure was tested to ultimate loads in a combined forward, sideward, and upward directions in accordance with CAR 3.390-2. The same loads were also applied in a downward direction by itself. The empennage was separated just aft of the aft pressure bulkhead but remained secured by flight control cables. According to personnel from the airplane manufacturer, the tested load (150 percent limit) for the empennage in negative shear translates to 14.0 g loading. Based on Cessna Engineering rough calculations, they believe the empennage is capable of sustaining an additional 30 percent beyond what it was tested to, or an estimated 18.2 g's in negative shear loading.

NTSB Probable Cause Narrative

The failure of the pilot to maintain airspeed (Vs) following a total loss of engine power from the right engine due to fuel starvation, resulting in an inadvertent stall, uncontrolled descent, and in-flight collision with trees and terrain. Factors in the accident was the failure pilot to feather the right propeller following the total loss of engine power, and his lack of total experience in the accident make/model of aircraft.

Event Information

Type of Event Accident
Event Date 6/26/2003
Event Day of the Week Thursday
Time of Event 1251
Event Time Zone Eastern Daylight Time
Event City N. Fort Myers
Event State FLORIDA
Event Country --
Zipcode of the event site 33903
Event Date Year 2003
Event Date Month 6
MidAir Collision Indicator No
On Ground Collision occurred ? No
Event Location Latitude 264441N
Event Location Longitude 0815606W
Event Location Airport --
Event Location Nearest Airport ID --
Indicates whether the acc/inc occurred off or on an airport Off Airport/Airstrip
Distance from airport in statute miles --
Degrees magnetic from airport --
Airport Elevation --
Weather Briefing Completeness --
Investigator's weather source Weather Observation Facility
Time of the weather observation 1253 Eastern Daylight Time
Direction of event from weather observation facility (degrees) --
Weather Observation Facility ID KFMY
Elevation of weather observation facility 17
Distance of event from weather observation facility (units?) --
Time Zone of the weather observation EDT
Lighting Conditions Day
Lowest Ceiling Height --
Lowest Non-Ceiling Height --
Sky/Lowest/Cloud Conditions Clear
Sky Condition for Lowest Ceiling None
Visibility Runway Visual Range (Feet) --
Visibility Runway Visual Value (Statute Miles) --
Visibility (Statute Miles) 10
Air Temperature at event time (in degrees celsius) 30
Dew Point at event time (in degress fahrenheit) 22
Wind Direction (degrees magnetic) 70
Variable Wind Indicator Wind direction could be determined
Wind Speed (knots) 7
Wind Velocity Indicator --
Wind Gust Indicator Not Gusting
Wind Gust (knots) --
Altimeter Setting at event time (in. Hg) 30.05
Density Altitude (feet) --
Intensity of Precipitation --
METAR weather report --
Event Highest Injury Fatal
On Ground, Fatal Injuries --
On Ground, Minor Injuries --
On Ground, Serious Injuries --
Injury Total Fatal 2
Injury Total Minor 1
Injury Total None --
Injury Total Serious 1
Injury Total All 4
Investigating Agency NTSB
NTSB Docket Number (internal use) 19572
NTSB Notification Source Lee County Port Authority
NTSB Notification Date Jun 26 2003 12:00AM
NTSB Notification Time 1334
Fiche Number and/or location -used to find docket information DMS
Date of most recent change to record Apr 25 2006 11:00AM
User who most recently changed record NTSB\JOHB
Basic weather conditions Visual Meteorological Cond
FAA District Office Tampa, Florida

Aircraft Involved

Aircraft #1

Aircraft Registration Number N749AA
NTSB Number MIA03FA135
Missing Aircraft Indicator --
Federal Aviation Reg. Part Part 91: General Aviation
Type of Flight Plan filed None
Flight plan Was Activated? No
Damage Substantial
Aircraft Fire None
Aircraft Explosion None
Aircraft Manufacturer's Full Name Cessna
Aircraft Model 414
Aircraft Series Identifier --
Aircraft Serial Number 414-0049
Certified Max Gross Weight 6200
Aircraft Category Airplane
Aircraft Registration Class U.S. Registered/U.S. Soil
Aircraft is a homebuilt? No
Flight Crew Seats --
Cabin Crew Seats --
Passenger Seats --
Total number of seats on the aircraft 8
Number of Engines 2
Fixed gear or retractable gear Retractable
Aircraft, Type of Last Inspection Annual
Date of Last Inspection Feb 1 2003 12:00AM
Airframe hours since last inspection --
Airframe Hours 1710.1
ELT Installed Yes
ELT Activated --
ELT Aided Location of Event Site No
ELT Type --
Aircraft Owner Name Osprey Air Services, Inc.
Aircraft Owner Street Address 3511 Silverside Road, Suite 105
Aircraft Owner City Wilmington
Aircraft Owner State DE
Aircraft Owner Country USA
Aircraft Owner Zipcode 19810
Operator is an individual? No
Operator Name John E. Nowicki Jr.
Operator Same as Owner? No
Operator Is Doing Business As --
Operator Address Same as Owner? No
Operator Street Address 6044 86th Terrace South
Operator City Lake Worth
Operator State FL
Operator Country USA
Operator Zip code 334676204
Operator Code --
Owner has at least one certificate None
Other Operator of large aircraft? --
Certified for Part 133 or 137 Operation --
Operator Certificate Number --
Indicates whether an air carrier operation was scheduled or not --
Indicates Domestic or International Flight --
Operator carrying Pax/Cargo/Mail --
Type of Flying (Per_Bus / Primary) Personal
Second Pilot on Board Yes
Departure Point Same as Event No
Departure Airport Code KLNA
Departure City West Palm Beach
Departure State FL
Departure Country USA
Departure Time 1213
Departure Time Zone EDT
Destination Same as Local Flt --
Destination Airport Code 94FL
Destination City Fort Myers
Destination State FL
Destination Country USA
Specific Phase of Flight Maneuvering
Report sent to ICAO? Yes
Evacuation occurred Yes
Date of most recent change to record Feb 3 2006 3:33PM
User who most recently changed record KENJ
Since inspection or accident Last Inspection
Event Location Runway Number and Location --
Runway Length --
Runway Width --
Sight Seeing flight No
Air Medical Flight No
Medical Flight --