Caldwell Industrial Airport
Aircraft Accident/Incident Report

Caldwell, Idaho 83605
Sunday, September 4, 2011 8:30 MDT

NTSB Narrative Summary Released at Completion of Accident

The builder/owner/pilot of the kit-built experimental airplane and his non-pilot-rated passenger flew from California to Idaho in order to attend the kit manufacturer’s fly-in and visit relatives. Two days before the accident, they flew to Idaho, and the next day they flew 4 hours. On the third day, the airplane was taxied from its parking spot on the ramp about 0740, and the pilot conducted a takeoff to about 50 feet, before landing straight ahead on the remaining runway. The investigation was unable to determine the purpose of this flight, or whether the passenger was on board at that time. The airplane was then taxied back to the ramp. About 13 minutes later, the airplane left the ramp again, taxied to the opposite runway, and began another takeoff roll. When the airplane was about 200 feet above the runway, the engine stopped developing power. The airplane stalled and spun to the ground, impacting on airport property near the departure end of the runway. Weight and balance calculations indicated that the airplane was likely 60 to 100 pounds above its maximum allowable weight, and that the center of gravity was about 1.7 inches forward of the aft limit, which would have increased the airplane pitch up tendency following the loss of engine power. Because the airplane was experimental and the pitch trim setting was unable to be determined during postaccident examination, the investigation was unable to determine whether there was sufficient control authority to prevent the stall and also what the required control forces would have been. Examination of the wreckage revealed that the two installed air filters had flow capacities well below the minimum value specified by the engine manufacturer, which would have limited the engine’s ability to develop its full rated power. However, this was not a factor in this accident, because the airplane had been flown successfully in the previous days. The engine was not equipped with carburetor heat, even though it was required by the engine manufacturer. When plotted on a carburetor icing chart, the ambient air temperature and dew point values indicated that conditions for serious carburetor icing at cruise power existed. The engine-driven fuel pump was too damaged to test, but the engine manufacturer noted that it should have been replaced in accordance with a 2007 Service Bulletin, which warned that excessively high fuel pressure could result in “engine malfunction and/or massive fuel leakage.” Although the possibility exists that the engine experienced a total loss of power due to carburetor icing, excessive fuel pressure, or a combination of the two, the investigation was unable to conclusively determine whether either caused the loss of engine power. Finally, no evidence of an angle-of-attack or stall warning system was observed in the wreckage. Although not required, such a system might have alerted the pilot of the impending stall and helped him avoid the stall and subsequent spin.

NTSB Probable Cause Narrative

The pilot’s failure to prevent a low-altitude stall and spin following a complete loss of engine power during the initial climb after takeoff.

Event Information

Type of Event Accident
Event Date 9/4/2011
Event Day of the Week Sunday
Time of Event 830
Event Time Zone Mountain Daylight Time
Event City Caldwell
Event State IDAHO
Event Country --
Zipcode of the event site 83605
Event Date Year 2011
Event Date Month 9
MidAir Collision Indicator No
On Ground Collision occurred ? No
Event Location Latitude 433831N
Event Location Longitude 1163808W
Event Location Airport Caldwell Industrial
Event Location Nearest Airport ID EUL
Indicates whether the acc/inc occurred off or on an airport On Airport
Distance from airport in statute miles 1
Degrees magnetic from airport --
Airport Elevation 2432
Weather Briefing Completeness --
Investigator's weather source Weather Observation Facility
Time of the weather observation 835 Mountain Daylight Time
Direction of event from weather observation facility (degrees) --
Weather Observation Facility ID EUL
Elevation of weather observation facility 2432
Distance of event from weather observation facility (units?) 0
Time Zone of the weather observation MDT
Lighting Conditions Day
Lowest Ceiling Height --
Lowest Non-Ceiling Height --
Sky/Lowest/Cloud Conditions Clear
Sky Condition for Lowest Ceiling None
Visibility Runway Visual Range (Feet) --
Visibility Runway Visual Value (Statute Miles) --
Visibility (Statute Miles) 10
Air Temperature at event time (in degrees celsius) 9
Dew Point at event time (in degress fahrenheit) 2
Wind Direction (degrees magnetic) 110
Variable Wind Indicator Wind direction could be determined
Wind Speed (knots) 5
Wind Velocity Indicator --
Wind Gust Indicator Not Gusting
Wind Gust (knots) --
Altimeter Setting at event time (in. Hg) 30.12
Density Altitude (feet) --
Intensity of Precipitation --
METAR weather report --
Event Highest Injury Fatal
On Ground, Fatal Injuries --
On Ground, Minor Injuries --
On Ground, Serious Injuries --
Injury Total Fatal 2
Injury Total Minor --
Injury Total None --
Injury Total Serious --
Injury Total All 2
Investigating Agency NTSB
NTSB Docket Number (internal use) 32489
NTSB Notification Source FAA NWM ROC
NTSB Notification Date --
NTSB Notification Time --
Fiche Number and/or location -used to find docket information --
Date of most recent change to record Dec 12 2013 4:21PM
User who most recently changed record huhm
Basic weather conditions Visual Meteorological Cond
FAA District Office --

Aircraft Involved

Aircraft #1

Aircraft Registration Number N624JS
NTSB Number WPR11FA428
Missing Aircraft Indicator --
Federal Aviation Reg. Part Part 91: General Aviation
Type of Flight Plan filed None
Flight plan Was Activated? No
Damage Substantial
Aircraft Fire None
Aircraft Explosion None
Aircraft Manufacturer's Full Name VEATCH
Aircraft Model KITFOX
Aircraft Series Identifier 7
Aircraft Serial Number S70302022
Certified Max Gross Weight 1320
Aircraft Category Airplane
Aircraft Registration Class --
Aircraft is a homebuilt? Yes
Flight Crew Seats --
Cabin Crew Seats --
Passenger Seats --
Total number of seats on the aircraft 2
Number of Engines 1
Fixed gear or retractable gear Fixed
Aircraft, Type of Last Inspection Conditional
Date of Last Inspection Nov 17 2010 12:00AM
Airframe hours since last inspection 42
Airframe Hours 162
ELT Installed Yes
ELT Activated Yes
ELT Aided Location of Event Site No
ELT Type C91
Aircraft Owner Name James Veatch
Aircraft Owner Street Address --
Aircraft Owner City Clayton
Aircraft Owner State CA
Aircraft Owner Country USA
Aircraft Owner Zipcode 94517
Operator is an individual? Yes
Operator Name James Veatch
Operator Same as Owner? Yes
Operator Is Doing Business As --
Operator Address Same as Owner? Yes
Operator Street Address --
Operator City Clayton
Operator State CA
Operator Country USA
Operator Zip code 94517
Operator Code --
Owner has at least one certificate None
Other Operator of large aircraft? --
Certified for Part 133 or 137 Operation --
Operator Certificate Number --
Indicates whether an air carrier operation was scheduled or not --
Indicates Domestic or International Flight --
Operator carrying Pax/Cargo/Mail --
Type of Flying (Per_Bus / Primary) Personal
Second Pilot on Board No
Departure Point Same as Event Yes
Departure Airport Code EUL
Departure City Caldwell
Departure State ID
Departure Country USA
Departure Time 830
Departure Time Zone MDT
Destination Same as Local Flt --
Destination Airport Code LOL
Destination City Lovelock
Destination State NV
Destination Country USA
Specific Phase of Flight --
Report sent to ICAO? --
Evacuation occurred --
Date of most recent change to record Dec 12 2013 5:22PM
User who most recently changed record huhm
Since inspection or accident Time of Accident
Event Location Runway Number and Location 30
Runway Length 5500
Runway Width 100
Sight Seeing flight No
Air Medical Flight No
Medical Flight --