Charles B. Wheeler Downtown Airport
Aircraft Accident/Incident Report

Kansas City, Missouri 64116
Sunday, August 18, 2013 14:48 CDT

NTSB Narrative Summary Released at Completion of Accident

The airplane experienced a total loss of engine power during takeoff from a runway that had a usable length of 6,827 feet; however, the pilot initiated the takeoff from a taxiway intersection, which left only about 5,313 feet of runway remaining. After the loss of engine power, the airplane descended to about 10 feet above ground level (agl) with the landing gear retracted; about half of the runway length remained. Engine power was restored, and the airplane subsequently climbed to between about 300 and 400 agl. The engine again lost power, and the airplane subsequently stalled and impacted a field. The landing gear remained retracted. Typically, the landing gear should be retracted after liftoff when the airplane has reached an altitude where, in the event of an engine failure or other emergency requiring an aborted takeoff, the airplane could no longer be landed on the runway. The airplane arrived at the departure airport 3 days before the accident and was parked on the ramp. It rained 1.22 inches during the 3 days the airplane was parked on the ramp. Examination of the airplane revealed the presence of water in the fuel diaphragm and fuel servo. No evidence of fuel contamination in the fuel pumps was found, and no reports of fuel contamination or engine power loss of airplanes that had been refueled from the fuel pumps before and after the accident were made. Examination of the fuel filler caps revealed that the cap components were in place and that both caps were in place and secure. When water was poured onto the fuel caps when they were placed and secured back into position, they exhibited leakage into the fuel tank; however, the extent of deformation around the filler neck due to accident damage was unknown. During the most recent annual inspection, it was noted that the fuel cap O-rings were replaced because of water contamination of the fuel system. No record was found indicating that maintenance personnel pressurized the fuel tanks to check for fuel cap leakage in accordance with the airplane manufacturer’s maintenance instructions. No internal obstruction was noted in the fuel system that would have precluded the pilot from detecting water in the system while sumping it during the preflight inspection.

NTSB Probable Cause Narrative

The pilot’s improper decision to attempt continued flight after a momentary loss of engine power with usable runway remaining. Contributing to the accident were the pilot’s premature retraction of the landing gear and the loss of engine power due to fuel system water contamination from precipitation, which resulted from maintenance personnel’s failure to comply with the manufacturer’s maintenance instructions and the pilot’s failure to detect fuel contamination during the preflight inspection.

Event Information

Type of Event Accident
Event Date 8/18/2013
Event Day of the Week Sunday
Time of Event 1448
Event Time Zone Central Daylight Time
Event City Kansas City
Event State MISSOURI
Event Country --
Zipcode of the event site 64116
Event Date Year 2013
Event Date Month 8
MidAir Collision Indicator No
On Ground Collision occurred ? No
Event Location Latitude 390643N
Event Location Longitude 0942136E
Event Location Airport Charles B. Wheeler Downtown
Event Location Nearest Airport ID MKC
Indicates whether the acc/inc occurred off or on an airport On Airport
Distance from airport in statute miles 0
Degrees magnetic from airport --
Airport Elevation 757
Weather Briefing Completeness --
Investigator's weather source Weather Observation Facility
Time of the weather observation 1454 Central Daylight Time
Direction of event from weather observation facility (degrees) 225
Weather Observation Facility ID MKC
Elevation of weather observation facility 757
Distance of event from weather observation facility (units?) 25
Time Zone of the weather observation CDT
Lighting Conditions Day
Lowest Ceiling Height --
Lowest Non-Ceiling Height --
Sky/Lowest/Cloud Conditions Clear
Sky Condition for Lowest Ceiling Broken
Visibility Runway Visual Range (Feet) --
Visibility Runway Visual Value (Statute Miles) --
Visibility (Statute Miles) 10
Air Temperature at event time (in degrees celsius) 28
Dew Point at event time (in degress fahrenheit) 14
Wind Direction (degrees magnetic) 140
Variable Wind Indicator Wind direction could be determined
Wind Speed (knots) 5
Wind Velocity Indicator --
Wind Gust Indicator Not Gusting
Wind Gust (knots) --
Altimeter Setting at event time (in. Hg) 30.1
Density Altitude (feet) --
Intensity of Precipitation --
METAR weather report --
Event Highest Injury Fatal
On Ground, Fatal Injuries --
On Ground, Minor Injuries --
On Ground, Serious Injuries --
Injury Total Fatal 2
Injury Total Minor --
Injury Total None --
Injury Total Serious --
Injury Total All 2
Investigating Agency NTSB
NTSB Docket Number (internal use) 33304
NTSB Notification Source CEN Duty Officer
NTSB Notification Date --
NTSB Notification Time --
Fiche Number and/or location -used to find docket information --
Date of most recent change to record Oct 15 2014 12:59PM
User who most recently changed record galm
Basic weather conditions Visual Meteorological Cond
FAA District Office --

Aircraft Involved

Aircraft #1

Aircraft Registration Number N9201R
NTSB Number CEN13FA496
Missing Aircraft Indicator --
Federal Aviation Reg. Part Part 91: General Aviation
Type of Flight Plan filed None
Flight plan Was Activated? No
Damage Substantial
Aircraft Fire None
Aircraft Explosion None
Aircraft Manufacturer's Full Name MOONEY
Aircraft Model M20J
Aircraft Series Identifier --
Aircraft Serial Number 24-0614
Certified Max Gross Weight 2740
Aircraft Category Airplane
Aircraft Registration Class --
Aircraft is a homebuilt? No
Flight Crew Seats --
Cabin Crew Seats --
Passenger Seats --
Total number of seats on the aircraft 4
Number of Engines 1
Fixed gear or retractable gear Retractable
Aircraft, Type of Last Inspection Annual
Date of Last Inspection Jan 8 2013 12:00AM
Airframe hours since last inspection --
Airframe Hours 2424
ELT Installed Yes
ELT Activated Unknown
ELT Aided Location of Event Site Unknown
ELT Type --
Aircraft Owner Name Air McRoyal LLC
Aircraft Owner Street Address --
Aircraft Owner City Youngstown
Aircraft Owner State OH
Aircraft Owner Country USA
Aircraft Owner Zipcode --
Operator is an individual? No
Operator Name Pilot
Operator Same as Owner? No
Operator Is Doing Business As --
Operator Address Same as Owner? No
Operator Street Address --
Operator City Girard
Operator State OH
Operator Country USA
Operator Zip code --
Operator Code --
Owner has at least one certificate None
Other Operator of large aircraft? --
Certified for Part 133 or 137 Operation --
Operator Certificate Number --
Indicates whether an air carrier operation was scheduled or not --
Indicates Domestic or International Flight --
Operator carrying Pax/Cargo/Mail --
Type of Flying (Per_Bus / Primary) Personal
Second Pilot on Board No
Departure Point Same as Event Yes
Departure Airport Code MKC
Departure City Kansas City
Departure State MO
Departure Country USA
Departure Time 1440
Departure Time Zone CDT
Destination Same as Local Flt --
Destination Airport Code --
Destination City Youngstown
Destination State OH
Destination Country USA
Specific Phase of Flight --
Report sent to ICAO? --
Evacuation occurred --
Date of most recent change to record Oct 15 2014 1:04PM
User who most recently changed record galm
Since inspection or accident Last Inspection
Event Location Runway Number and Location 19
Runway Length 6827
Runway Width 150
Sight Seeing flight No
Air Medical Flight No
Medical Flight --