N/A Airport
Aircraft Accident/Incident Report

Owasso, Oklahoma 74055
Sunday, November 10, 2013 15:46 CST

NTSB Narrative Summary Released at Completion of Accident

Radar and air traffic control communications indicated that the Mitsubishi MU-2B-25 was operating normally and flew a nominal flightpath from takeoff through the beginning of the approach until the airplane overshot the extended centerline of the landing runway, tracking to the east and left of course by about 0.2 nautical mile then briefly tracking back toward the centerline. The airplane then entered a 360-degree turn to the left, east of the centerline and at an altitude far below what would be expected for a nominal flightpath and intentional maneuvering flight given the airplane's distance from the airport, which was about 5 miles. As the airplane was in its sustained left turn tracking away from the airport, the controller queried the pilot, who stated that he had a "control problem" and subsequently stated he had a "left engine shutdown." This was the last communication received from the pilot. Witnesses saw the airplane spiral toward the ground and disappear from view. Examination of the wreckage revealed that the landing gear was in the extended position, the flaps were extended 20 degrees, and the left engine propeller blades were in the feathered position. Examination of the left engine showed the fuel shutoff valve was in the closed position, consistent with the engine being in an inoperative condition. As examined, the airplane was not configured in accordance with the airplane flight manual engine shutdown and single-engine landing procedures, which state that the airplane should remain in a clean configuration with flaps set to 5 degrees at the beginning of the final approach descent and the landing gear retracted until landing is assured. Thermal damage to the cockpit instrumentation precluded determining the preimpact position of fuel control and engine switches. The investigation found that the airplane was properly certified, equipped, and maintained in accordance with federal regulations and that the recovered airplane components showed no evidence of any preimpact structural, engine, or system failures. The investigation also determined that the pilot was properly certificated and qualified in accordance with applicable federal regulations, including Special Federal Aviation Regulation (SFAR) No. 108, which is required for MU-2B pilots and adequate for the operation of MU-2B series airplanes. The pilot had recently completed the SFAR No. 108 training in Kansas and was returning to Tulsa. At the time of the accident, he had about 12 hours total time in the airplane make and model, and the flight was the first time he operated the airplane as a solo pilot. The investigation found no evidence indicating any preexisting medical or behavioral conditions that might have adversely affected the pilot's performance on the day of the accident. Based on aircraft performance calculations, the airplane should have been flyable in a one-engine-inoperative condition; the day visual meteorological conditions at the time of the accident do not support a loss of control due to spatial disorientation. Therefore, the available evidence indicates that the pilot did not appropriately manage a one-engine-inoperative condition, leading to a loss of control from which he did not recover. The airplane was not equipped, and was not required to be equipped, with any type of crash-resistant recorder. Although radar data and air traffic control voice communications were available during the investigation to determine the airplane's altitude and flightpath and estimate its motions (pitch, bank, yaw attitudes), the exact movements and trim state of the airplane are unknown, and other details of the airplane's performance (such as power settings) can only be estimated. In addition, because the airplane was not equipped with any type of recording device, the pilot's control and system inputs and other actions are unknown. The lack of available data significantly increased the difficulty of determining the specific causes that led to this accident, and it was not possible to determine the reasons for the left engine shutdown or evaluate the pilot's recognition of and response to an engine problem. Recorded video images from the accident flight would possibly have shown where the pilot's attention was directed during the reported problems, his interaction with the airplane controls and systems, and the status of many cockpit switches and instruments. Recorded flight data would have provided information about the engines' operating parameters and the airplane's motions. Previous NTSB recommendations have addressed the need for recording information on airplane types such as the one involved in this accident. Recorders can help investigators identify safety issues that might otherwise be undetectable, which is critical to the prevention of future accidents.

NTSB Probable Cause Narrative

The pilot's loss of airplane control during a known one-engine-inoperative condition. The reasons for the loss of control and engine shutdown could not be determined because the airplane was not equipped with a crash-resistant recorder and postaccident examination and testing did not reveal evidence of any malfunction that would have precluded normal operation.

Event Information

Type of Event Accident
Event Date 11/10/2013
Event Day of the Week Sunday
Time of Event 1546
Event Time Zone Central Standard Time
Event City Owasso
Event State OKLAHOMA
Event Country --
Zipcode of the event site 74055
Event Date Year 2013
Event Date Month 11
MidAir Collision Indicator No
On Ground Collision occurred ? No
Event Location Latitude 361751N
Event Location Longitude 0955228W
Event Location Airport N/A
Event Location Nearest Airport ID --
Indicates whether the acc/inc occurred off or on an airport Off Airport/Airstrip
Distance from airport in statute miles 5
Degrees magnetic from airport 360
Airport Elevation --
Weather Briefing Completeness --
Investigator's weather source Weather Observation Facility
Time of the weather observation 1553 Central Standard Time
Direction of event from weather observation facility (degrees) 180
Weather Observation Facility ID TUL
Elevation of weather observation facility --
Distance of event from weather observation facility (units?) 5
Time Zone of the weather observation CST
Lighting Conditions Day
Lowest Ceiling Height --
Lowest Non-Ceiling Height 9000
Sky/Lowest/Cloud Conditions Scattered
Sky Condition for Lowest Ceiling None
Visibility Runway Visual Range (Feet) --
Visibility Runway Visual Value (Statute Miles) --
Visibility (Statute Miles) 10
Air Temperature at event time (in degrees celsius) 19
Dew Point at event time (in degress fahrenheit) 6
Wind Direction (degrees magnetic) 140
Variable Wind Indicator Wind direction could be determined
Wind Speed (knots) 6
Wind Velocity Indicator --
Wind Gust Indicator Not Gusting
Wind Gust (knots) --
Altimeter Setting at event time (in. Hg) 30.26
Density Altitude (feet) --
Intensity of Precipitation --
METAR weather report KTUL 102153Z 14006KT 10SM SCT090 19/06 A3026 RMK A
Event Highest Injury Fatal
On Ground, Fatal Injuries --
On Ground, Minor Injuries --
On Ground, Serious Injuries --
Injury Total Fatal 1
Injury Total Minor --
Injury Total None --
Injury Total Serious --
Injury Total All 1
Investigating Agency NTSB
NTSB Docket Number (internal use) 32982
NTSB Notification Source FAA
NTSB Notification Date --
NTSB Notification Time --
Fiche Number and/or location -used to find docket information --
Date of most recent change to record Nov 18 2013 12:20PM
User who most recently changed record saua
Basic weather conditions Visual Meteorological Cond
FAA District Office --

Aircraft Involved

Aircraft #1

Aircraft Registration Number N856JT
NTSB Number CEN14FA046
Missing Aircraft Indicator --
Federal Aviation Reg. Part Part 91: General Aviation
Type of Flight Plan filed IFR
Flight plan Was Activated? Yes
Damage Destroyed
Aircraft Fire Ground
Aircraft Explosion None
Aircraft Manufacturer's Full Name MITSUBISHI
Aircraft Model MU 2B-25
Aircraft Series Identifier --
Aircraft Serial Number 306
Certified Max Gross Weight 9920
Aircraft Category Airplane
Aircraft Registration Class --
Aircraft is a homebuilt? No
Flight Crew Seats 2
Cabin Crew Seats 5
Passenger Seats 7
Total number of seats on the aircraft 7
Number of Engines 2
Fixed gear or retractable gear Retractable
Aircraft, Type of Last Inspection Continuous Airworthiness
Date of Last Inspection Sep 19 2013 12:00AM
Airframe hours since last inspection 13
Airframe Hours 6581
ELT Installed Yes
ELT Activated No
ELT Aided Location of Event Site Unknown
ELT Type Unknown
Aircraft Owner Name Anasazi Winds, LLC
Aircraft Owner Street Address --
Aircraft Owner City Tulsa
Aircraft Owner State OK
Aircraft Owner Country USA
Aircraft Owner Zipcode --
Operator is an individual? Yes
Operator Name ON FILE
Operator Same as Owner? No
Operator Is Doing Business As --
Operator Address Same as Owner? No
Operator Street Address --
Operator City Tulsa
Operator State OK
Operator Country USA
Operator Zip code --
Operator Code --
Owner has at least one certificate None
Other Operator of large aircraft? --
Certified for Part 133 or 137 Operation --
Operator Certificate Number --
Indicates whether an air carrier operation was scheduled or not --
Indicates Domestic or International Flight --
Operator carrying Pax/Cargo/Mail --
Type of Flying (Per_Bus / Primary) Personal
Second Pilot on Board No
Departure Point Same as Event No
Departure Airport Code SLN
Departure City Salina
Departure State KS
Departure Country USA
Departure Time 1500
Departure Time Zone CST
Destination Same as Local Flt --
Destination Airport Code TUL
Destination City Tulsa
Destination State OK
Destination Country USA
Specific Phase of Flight --
Report sent to ICAO? --
Evacuation occurred --
Date of most recent change to record May 19 2014 5:05PM
User who most recently changed record saua
Since inspection or accident Last Inspection
Event Location Runway Number and Location N/A
Runway Length --
Runway Width --
Sight Seeing flight No
Air Medical Flight No
Medical Flight --