NTSB Narrative Summary Released at Completion of Accident
On October 12, 2014 about 1250 eastern daylight time, a Cessna 180K, N2590K, was substantially damaged when it nosed over during a forced landing after a loss of engine power in Boca Raton, Florida. The private pilot received minor injuries. The passenger was uninjured. The flight departed from Columbus Airport (CSG), Columbus, Georgia, about 0930, destined for Boca Raton Airport (BCT), Boca Raton, Florida. Visual meteorological conditions prevailed, and an IFR flight plan was filed for the personal flight, conducted under the provisions of Title 14 Code of Federal Regulations Part 91.
According to the pilot, on the day before the accident occurred, he and his wife had departed Southwest Michigan Regional Airport (BEH), Benton Harbor, Michigan, at approximately 1015 then flew approximately 1.5 hours to Monroe County Airport (BMG), Bloomington, Indiana for fuel. After landing at BMG, they had the airplane refueled, filling the tanks with 24 gallons of fuel and then departed for CSG. After flying 3.2 hours, they landed at CSG. The pilot then had the airplane refueled once again, topping the fuel tanks off with 54.3 gallons of fuel and then checked in to a hotel.
The following morning, the pilot and his wife returned to CSG from the hotel and departed for BCT at approximately 0930. The pilot advised that the flight was very pleasant with some clouds and build up near Sebring, Florida and that he had entered and flown in instrument meteorological conditions for approximately 42 minutes while at their cruising altitude of 5,000 feet above mean sea level (msl) without any problems. As they were handed off to Palm Beach Approach, they descended to 4,000 feet msl, and were gradually descended down to 2,000 feet msl. A little while later after leveling at 2,000 feet msl they were cleared to 1,000 feet msl. and were handed off to BCT control tower. Moments later, the airplane began shaking violently, a "loud noise" was heard, and the propeller stopped rotating, and then began windmilling slowly. The engine however, would not produce any power. The tower then cleared them for a visual approach to runway 05.
The pilot realized that they were not going to make the airport and he and his wife began looking for an "open area" to make an "engine out" landing while he trimmed the airplane and tried to restart the engine. He then spotted what used to be a polo field which was being developed into home sites and turned towards it. He thought it was his only chance to land in an unobstructed area. His wife meanwhile spotted "wires" and advised him of them while he continued to fly the airplane and attempted to restart the engine. Then after clearing the last of the "wires" he turned the airplane to align it with the polo field and landed. The ground was soft and sandy however, and during the landing roll, the airplane nosed over and came to rest inverted. The pilot and his wife then released their safety harnesses and egressed.
A preliminary examination by a Federal Aviation Administration Inspector indicated that the vertical stabilizer was substantially damaged.
The airplane has been retained by the NTSB for further examination.